Where possible I've tried
to include all the problems and frustrations encountered in building
the kit. I've also included the solutions to the problems, which, while
not always very technical might help other builders of G27 kits.
Friday 1/10/99
Kit delivered during the morning.
Not all components that should have been with the stage 1 kit actually
arrived. Notable omissions from the kit were:
- One alloy wheel
- Prop shaft
- 10 out 14 rear suspension bushes
- Carburettor idle jets
- Coolant header tank
- Top radiator hose
- Radiator fan assembly
- Fan belt
- Fuel line
- Brake pipe to master cylinder
- Various nuts, bolts, washers etc.
Decided to lay out all components
on garage floor around the chassis to take first photographs of build
and to confirm any missing components.
Nut and bolt pack opened up
and bolts assigned to various components. It soon became apparent that
a number of bolts were missing and some supplied were too short (e.g.)
front lower ball joint bolts too short.
Saturday 2/10/99
Full bolt count carried out and
email sent to Ginetta detailing missing parts.
Steering rack was fitted to
chassis but thread on "U" brackets is very poor and will require
changing before completion of car. It was decided not to do anything
about the threads at this point as the rack would have to be bolted
and unbolted numerous times during the steering set up stage.
Top wishbone holes required
drilling out as these were supplied threaded and should have been plain.
Built up offside front suspension
except for lower ball joint that requires longer bolts.
Problem: Stripped thread
on lower wishbone mounting on front nearside due to using the nut to
pull the bolt through the hole in the chassis plate.
Solution: All chassis
holes were drilled out to the correct diameter to remove the powder
coating which prevented many of the bolts being fitted. I would recommend
that anyone who receives powder coated or galvanised parts drills out
holes before attempting to assemble them.
Thursday 7/10/99
Tried to contact Ginetta regarding
missing components but no joy.
Assembled rear hub to cast
upright and fitted drive shaft coupling.
Start made on assembling differential
mounting brackets and identified more missing M12 bolts.
Friday 8/10/99
Fitted the 4 off rear suspension
bushes that had arrived with the kit to the lower offside wishbone.
Dismantled rear brake calliper
to fit new brake pads.
Problem: Up to now
the build has gone OK but the Ginetta manual, though looking very good,
is short on some basic information.
Solution: Arranged
to visit Ginetta on Monday armed with a camera to take detailed photos
of a car currently under construction at the factory. I could also pick
up the missing parts from the kit.
Saturday 9/10/99
Assembled pedal box on loose
bolts to check that all parts were there prior to visiting Ginetta on
Monday. Surprise, surprise some parts were missing.
Sunday 10/10/99
Fitted brake pads to both front
callipers and found one of the callipers seized. Yet another parts problem
for Ginetta to sort out for me.
Monday 11/10/99
Drove to Sheffield to take photos
of car being built, sorted out some of the parts needed at S&T Motors
but had to wait for Martin to arrive to go to Hoyland for remaining
parts.
Came back with bolt pack,
fan, one alloy wheel, 10 suspension bushes, new brake calliper, top
radiator hose, fuel and brake lines plus an assortment of clips etc.
However still no idle jets,
fan belt, prop shaft or coolant header tank
On arrival home took wheels
and tyres for fitting and balancing.
Tuesday 12/10/99
Modified M12 bolts for fitting
diff to mounting brackets. Diff was fitted to chassis after drilling
out (slotting) front mounting holes in chassis plate.
Changed out lower front wishbone
bolt that was previously stripped. Fitted clamping bolts to upper ball
joint adapters.
Saturday 16/10/99
Fitted front offside brake disc
and calliper to hub.
Fitted bushes to all rear
suspension arms
Monday 18/10/99
At last, a day when it seemed
I was making good progress.
Left rear hub split and fitted
to cast upright. All wishbones fitted and bolts fitted loosely. Brake
discs fitted to both rear wheels and camber adjustment set to ensure
discs were vertical. Rear toe in adjuster not fitted yet due to needing
to machine 1/4" off each spacer to prevent fouling inside of wheels.
Rear wheels fitted, its starting
to look like a car!
Front nearside brake disc
and calliper fitted to hub. Bolts for bottom ball joint and shock absorber
mountings changed for correct length bolts. Shocks, springs and front
wheels fitted, yes it really is starting to look like a car!
Saturday 30/10/99
Back to working on the car at
last!
Problem: Set up rear
suspension toe in as per the Ginetta manual but found that at its lowest
point the brake calliper fouls the shock absorber. Checked correct fitting
of calliper as per the Ginetta manual and it looks right. Manual says
that cast uprights are not interchangeable so calliper must fit to the
front of the disc.
Solution: Rang Ginetta,
they didn't know what I was talking about as they always fit the calliper
to the rear because it fouls the shock absorber if fitted to the front.
(So why not change the instruction in the manual you might think?
..
I suspect thats too easy).
A bit fed up at this stage
I decided to leave the rear suspension for a while and concentrate on
fitting the engine and gearbox together and fit the starter motor and
alternator bracket. I then moved on to splitting the drive shaft couplings
for overhaul. As expected the bolts refused to move so they got a good
soak in easing oil and I got a good soak in the bath.
Sunday 31/10/99
Drive shaft couplings came apart
with the help of a large hammer. The c/v joints were completely dismantled
and degreased.
Monday 1/11/99
Repacked c/v joints with grease
and fitted new gaiters and clips. When fitting to the modified drive
shafts supplied by Ginetta another quality control problem was found.
It seemed as though whoever shortens the drive shafts for Ginetta holds
them tightly in a vice by the very end of the splined shaft.
Problem: The splined
ends of the drive shafts were so badly burred over that it was not possible
to pass the shaft through the couplings.
Solution: Very tediously
with a small file each spline was recut on the end of the drive shafts
Rear cast uprights were swapped
over from left to right and vice versa to allow fitting of the brake
callipers to the rear of the discs.
*Note It is important
to ensure that the correct drive stub shaft is fitted to the hub as
one has a right hand thread and the other a left for fitting of the
hub retaining nut.
Tuesday 2/11/99
Drive shaft fitted to offside
and rear wheel alignment carried out on both rear wheels. On completion
the suspension was jacked up to normal ride height and all bolts were
tightened.
Brake callipers were fitted
to both rear wheels and bolts torqued up to Ford spec. Brake flexi pipes
were fitted to callipers.
Wheel hub to cast upright
bolts were torqued up to Ford spec.
Rear springs and shock absorbers
fitted.
Track rod end fitted to nearside
of steering rack and rough alignment made to nearside wheel. Taking
suspension through full travel showed that steering rack needed raising
by packing with shims.
In trying to fit the track
rod end to the offside of the rack it was found that the modified track
rod end supplied by Ginetta had no thread cut in it.
Telephoned Ginetta who put
a replacement in the post straight away
Thursday 4/11/99
Drive shaft fitted to nearside
rear wheel
Fitted 3 way union to rear
of chassis and ran in brake pipes to rear flexi pipes. Brake line run
and clipped along inside of chassis rail to engine bay. 4 way union
was fitted to offside of chassis in engine bay to take brake light switch
and pipes to front brake flexi pipes. Metal brake pipe was bent to shape
and clipped along chassis to nearside but pipe to offside needs to be
shortened.
Fuel line run from rear of
chassis to engine bay and clipped along nearside chassis rail. Fuel
tank was placed in position and connected to the fuel line. Sender unit
fitted to the fuel tank. Chassis was drilled to take fuel tank retaining
straps and the retaining straps were shortened to allow easier fitting
of bolts. The straps were painted for fitting later.
The engine and gearbox assembly
was then fitted to the chassis. Rather than hire in an engine hoist
to lift the engine into place it was easier and cheaper to slide the
engine under the chassis then drop the chassis to the floor. As I already
had the engine supported on a wooden pallet on castors it was a simple
job to move the engine into position. With very little weight on the
front of the chassis (wheels etc. removed) it was easily lifted over
the engine. The only items needing removal to allow the engine to slot
into place were the oil filter and fuel pump.
Friday 5/11/99
Chassis raised again to place
on axle stands for fitting of gearbox mounting plate.
New track rod end arrived
and was fitted to offside of steering rack. The suspension was put through
its full travel and showed that the rack needed to be raised. Shims
were cut from alloy plate and suspension retried. Set up steering for
zero "toe in". Even with 9mm of shims on both sides of the
rack it still toes in slightly with the suspension raised.
At this point I decided to
contact the Ginetta owners club via the internet for advice on setting
up the rack.
Tuesday 9/11/99
Completed fuel line run to engine
bay and fitted flexible hose to the fuel pump and in-line fuel filter.
Gearbox was bolted into the
Ford rubber mount,
Problem: Had another
go at setting up the steering rack and as expected the threads stripped
on the steering rack retaining brackets.
Solution: I cut off
the existing studs from the retaining brackets and drilled out the clamps
to 8mm. I then fitted some M8 stud bar in the holes and tack welded
them into place.
The alternator was fitted
to the upside down alternator bracket and the offset from the crankshaft
pulley was measured.
Fitted shortened brake pipe
to front offside calliper.
Started to fit the radiator
assembly by fitting the fan to the radiator and the top hose to the
engine.
Problem: When fitting
the radiator to the brackets provided on the chassis, the bottom hose
fouls the steering rack. The radiator needed raising approx. 1.5"
to allow for fitting of the hose.
Solution: Stainless
steel Tee brackets were purchased from the local hardware shop and bent
into shape. These were then drilled and riveted to the chassis.
Wednesday 10/11/99
Radiator fitted to Tee brackets
and bottom radiator hose fitted in position. Bottom hose was cut to
length and refitted.
Problem: Just me being
a bit thick. When I cut the hose to length I forgot to allow for the
fan belt which now meant that the fan belt would pass right through
the middle of the hose.
Solution: Easy really
.buy
a new hose.
Fuel line run to engine bay
was modified slightly as I felt it was too close to the starter motor.
Inlet manifold and carburettors
fitted and rubber fuel lines cut to length.
Thursday 11/11/99
Tried to torque up the rear hub
retaining nuts but no joy as it was almost impossible to stop the opposite
rear wheel from turning. Decided to leave this job until the braking
system was complete and that would help stop the wheels from spinning.
Friday 12/11/99
Torqued up all front suspension
bolts except for track rod ends that will need further adjustment when
I get this steering rack height problem sorted.
Sunday 14/11/99
Removed alternator and bracket
and cut off excess metal which was fouling the bottom radiator hose.
Carried out final set up of
steering "toe in" now that full weight of chassis is on the
suspension.
Final tightening of rear drive
shaft "star drive" bolts was carried out.
Drilled out holes on speedometer
detector plate that fits between the prop shaft and the diff.
Problem: Me being thick
again. I assumed that the holes in the flange were an equal distance
apart, but they're not.
Solution: Not pretty
but 2 of the 4 holes required slotting by 1/4" by filing out with
a small round file.
Now waiting for the stage
2 (body, trim, electrics, options) kit to arrive
Wednesday 8/12/99
Body kit which was to arrive
at around 2:00 pm actually arrived at 6:00 pm, better late than never.
As I was due to start my night shift at 6:30 pm the shift manager who'd
already been on duty for 12 hours was less than impressed when I rang
to say I'd be late.
After offloading the kit from
the van it was obvious that a number of key parts were missing. Should
I be surprised?
.No!
Friday 10/12/99
The bodyshell had been laid loosely
on the chassis when delivered so the first job was to roll the whole
thing out onto the drive and lift off the body tub. Back in the garage
the bodyshell was propped up against the wall to gain access to the
underside to enable cutting of holes in the boot floor for the fuel
filler neck and tank sender unit. I also used this opportunity to cut
the holes in transmission tunnel for the handbrake lever and the bulkhead
for the steering column. Mistake coming up but more on that later.
The chassis rails were drilled
to accept the M6 body mounting bolts and the prop shaft was fitted ensuring
that the speedo detector plate was fitted between the flanges.
The chassis was rolled back
into the garage and the body was lifted into position with the assistance
of my neighbour Trevor and his sons Ian and Mark.
Drilled up through holes in
chassis rails through the sills and secured the body with M6 bolts
Monday 13/12/99
Handbrake lever modified slightly
to allow it to sit horizontal on the transmission tunnel. Handbrake
cable was secured loosely and various runs of the cable were tried to
get the best fit. I was not convinced that the way in which the cable
connects to the caliper under the rear suspension spacer looked right
so rang Ginetta to confirm how they run the cables on their turnkey
cars. The way I had run it was the same as Ginetta and they confirmed
that this did not pose a problem with the SVA examiner provided the
outer sheath cannot be chaffed by moving parts.
Hole cut in transmission tunnel
to allow the fitting of the gear lever.
Rear Bulkhead drilled trough
and secured bulkhead to chassis.
Tuesday 14/12/99 (Black
Tuesday)
Referring to the Ginetta build
manual for guidance the front bulkhead was marked up to accept the pedal
box arrangement.
The engine side of the bulkhead
was measured up and the steel bracket fixed to the bulkhead. Using the
plate as a template I proceeded to drill holes down through the chassis
and through the bulkhead for mounting the master cylinders. A slot was
also cut in the floor to accept the clutch pedal. Moving to the inside
of the car the pedal box was installed and the master cylinders bolted
up.
Problem: It very soon
became obvious that the pedal box was mounted around 50mm too close
to the transmission tunnel and it was impossible to operate the clutch
without my left foot catching the brake.
Solution: You'd have
thought by now I'd have learned to ignore the Ginetta manual or at the
very least to seriously question every dimension given. The complete
pedal box/master cylinder assembly was removed and the bulkhead was
re-fibre glassed to cover the holes previously cut. Measurements were
taken which would allow the brake pedal to sit central in the footwell
and the bulkhead marked up accordingly. Ginettas measurements were 12mm
from the transmission tunnel to the edge of the engine side bracket,
my own measurements made that dimension 60mm (not exactly a fine tolerance).
Tuesday 21/12/99
Completed fibre glassing the
front bulkhead to repair the aborted pedal box installation.
Dashboard support frame was
cut to size as per the Ginetta manual (after I'd checked the dimensions).
Problem: The frame
was offered up to the body and it became obvious that the frame couldn't
be fitted horizontal given the location of the brackets bonded into
the windscreen pillars. The brackets were measured up and the nearside
bracket sat a full 50mm lower then the offside bracket.
Solution: After trial
fitting to gauge which of the nearside or offside brackets was in the
correct position a small extension bracket was made up to raise the
nearside and allow the support frame to be fitted horizontal.
The bulkhead was re-cut to
allow fitting of the pedal box and the master cylinders were bolted
into place.
Wednesday 22/12/99
Pedal box fitted and seat fitted
loosely to enable a trial operation of the pedal assembly. Looks fine
except for one thing.
Problem: When operating
the clutch pedal my left foot totally obscured the hole cut in the bulkhead
for the steering column to exit. Trial fitting the steering column confirmed
that I either had to chop off my toes or mount the column higher.
Solution: Check the
measurements given in the Ginetta manual then add the obligatory 50mm
tolerance and re-cut the hole for the column 50 mm higher. Glass fibre
the previous hole (I needed the practice anyway).
Called it a day (and a millennium)
and went to collect a pair of 10 mm steering rack spacers which I'd
had made up.
Monday 3/1/00 Happy
New
Year!
Trimmed
fibreglass dash panel at edges to fit into recess.
Rear bodywork
cut outs made for rear lights also cut out made in rear for fuel filler
and the filler neck was fitted into the bodywork.
Brake pipe
from master cylinder to front 4 way adaptor fitted
New hole cut
in front bulkhead for steering column.
Problem:
While pushing the car forward out of the garage to give better access
to the rear lights I noticed that the gearbox was not in neutral. Obviously
it shouldn't have been possible to wheel the car forward. A quick look
under the car confirmed that everything looked in order but there was
no free play at all on the clutch release fork. Having bought a reconditioned
mechanical package from Ginetta I hadn't done the build up of the clutch
and flywheel but releasing the bell housing bolts slightly did release
the clutch.
Solution:
Split the bell housing from the engine just far enough to ensure the
clutch release bearing hadn't come of its guide during assembly. This
was done but everything looked normal. The engine / gearbox had to come
out again. (see later)
Tuesday
4/1/00
Flexible
brake pipes connected from fluid reservoir to master cylinders and system
filled with fluid. bleeding will be done later.
Friday
7/1/00
Contacted
various local tool hire companies to hire an engine hoist, during the
initial fitting of the engine the body wasn't fitted so the chassis
had been lifted over the top of the engine to allow fitting without
a hoist. This time with the body in place a hoist was a must. Can get
one for next Monday.
Started to
disconnect all ancillaries ready for engine to come out.
Monday
10/1/00
Hoist duly
arrived and with the help of my friend John Hickford the engine was
out of the car and sat on the garage floor inside 20 minutes. With the
engine out and the bell housing split a number of measurements were
taken. It soon became obvious that this set up was never going to work.
It was noticed also that the starter motor gear could not possibly mate
with the flywheel ring gear, this led me to believe that when Ginetta
built up the engine they fitted the wrong flywheel. After a few phone
calls to Ginetta and various measurements exchanged we concluded that
the flywheel was correct but the starter motor supplied was for a Zetec
not a Pinto and the clutch release fork supplied was for a V6.
Ginetta put
a new clutch release fork and starter motor in the post the following
day and these duly arrived on Wednesday
Wednesday
12/1/00
Clutch release
fork was fitted along with a new clutch release bearing (just in case
the original had been damaged earlier) and the starter motor was trial
fitted. Everything looking good.
John came
around again to help in the refitting of the engine and box. All went
very smoothly though one of us had to work from beneath to guide the
prop shaft splines into place while the whole unit was pushed back.
This was because the prop shaft hadn't been split from the diff due
to poor access to the bolts.
Slightly more
fiddly was realigning the gearbox rubber mounting onto the chassis brackets.
All in all a fairly easy job which is reassuring if I ever need to take
the engine / box unit out again in future.
Friday 14/1/00
Started to bleed the braking
system. Going well except for the handbrake doesn't appear to be holding
on the offside rear wheel. Pedal also feels a little spongy, will have
another go next week.
Removed dash panel and marked
out for instrument and warning lights using alloy panel as a template.
Monday 17/1/00
Contacted local VRO regarding
registration who will visit tomorrow afternoon.
Tuesday 18/1/00
VRO unable to come will call
tomorrow
Wednesday 19/1/00
VRO official called and allocated
a VIN (chassis) number. He also confirmed that under the current points
scheme he believed I would be allocated a new registration (i.e.) V
reg or W reg if registered after March 1st.
Thursday 20/1/00
Swapped temperature sender on
engine for the one supplied with the gauge.
Filled gearbox with oil
Bled front brake system and
had another go at the rear. Pedal weight is now OK but I still cant
get the handbrake to hold on the offside caliper.
Placed windscreen over the
aperture and marked out for cutout. Allowed 5mm clearance all round.
Trimmed aperture to size and fitted weather seal.
Friday 21/1/00
Collected high tensile steel
bolts for seat belt mountings and also aselection of other useful nuts
and bolts etc.
Collected new gear knob from
local motor factors
Had to remove rear caliper
to overhaul the auto brake adjustment system as still no joy getting
the handbrake to hold. Now OK after overhaul.
Put together wiper mechanism
and aligned roughly on scuttle to mark for position.
Monday 24/1/00
Cut out (trimmed) offside door
aperture and taped door into position to estimate final position.
Tuesday 25/1/00
Fitted wiper spindles to scuttle.
Despite being ultra careful with the drill and taping over everything
in sight to avoid scratching the body I scratched the scuttle with the
tip of a file
..bugger.
Fitted rear Ford Puma indicator
lamps
Fitted new clevis pin to handbrake
yolk
Wednesday 26/1/00
Final torque of the rear hub
nuts after borrowing a large torque wrench and socket from work.
Drilled bulkhead for fitting
of the wiper motor
Fitted bootlid hinges to body
and marked out bootlid for fitting of hinge brackets.
Sunday 30/1/00
Collected choke linkage for the
carbs from a friend. Fitted choke lever then installed choke cable from
dash to carbs.
Monday 31/1/00
Car pushed out onto drive to
carry out trial fit of the bonnet. Bonnet then removed and initial trim
of rear flange was carried out.
While the car was on the drive
I used the extra space to finish the fitting of the heater and connect
up the hoses. The coolant system was then filled with water/anti freeze
mix and checked for leaks.
Tuesday 1/2/00
Made a start on the dashboard
wiring. Main area worked on was around the Sierra column stalk switches.
Main engine bay wiring loom
was laid in position and connected where possible
Heater facia plate was fitted
to centre console
Hooray!
some more
parts arrived. Bonnet bolts, green indicator repeater lamps, fog and
fan override switches.
Wednesday 2/2/00
Completed the dashboard wiring
except for the fan and fog light switches. Panel light supply and earth
connections also still to sort.
Battery clamps fabricated
and fitted.
Battery earth connections
completed.
Thursday 3/2/00
Engine bay wiring completed including
fitting of the electronic ignition module to the nearside front suspension
turret. It should be free from damp tucked away behind the radiator.
All relays were fitted after
modifying the wiring to the relay panel as instructed in the wiring
harness literature.
All fuses fitted and all circuits
tested. 2 loose connections found on main wiper stalk plug, hazard warning
and horn circuits were crossed over due to difficulty in identifying
the difference between purple and brown wires.
Also found that wipers park
in the wrong direction. Slight modification to the wiper motor wheel
box will be needed.
Bonnet fitted roughly, will
require further alignment later.
Bonnet release catches were
to be fitted now but I was unable to drill them as they were case hardened.
Surface of metal will be ground off later.
Friday 4/2/00
Wiring completed to all panel
lights. Additional cable run in to accommodate oil pressure warning
light as well as oil pressure gauge.
Fabricated throttle linkage
and fitted it to the carbs.
Washer bottle and pump was
fitted to nearside of chassis just ahead of the passenger door.
Major tidy up of garage carried
out as I was starting to have difficulty in finding various bits and
pieces under all the rubbish.
Sunday 6/2/00
Offside headlamp fitted
Monday 7/2/00
Martin Dawson from S&T Motors
came up to deliver side screens and new clutch cable. We talked through
the remaining problems with the build. At this point we identified that
some of the parts supplied for the door locks were incorrect.
Nearside headlamp fitted.
Friday 11/2/00
Wiper motor wheel box modified
to give correct park position for wipers
Case hardening on bonnet catches
ground off and drilled out for attaching the release cable.